Treaty Energy Corporation has cased and cemented the Stockton #2 well in Tuscola, Texas with positive initial results.
The Company began drilling the Stockton #2 well on September 27, 2013. At roughly 8:20AM on October 08, 2013 the drilling operation reached a total depth of 4,783ft. after visible signs of hydrocarbons in the mud pits.
A top-to-bottom wire line log was conducted which, as anticipated, confirmed two pay zones in the well located at 4,075ft. and 4,490ft. with the pay zone sizes being 25ft. and 8ft., respectively. The Stockton #2 well shares a similar pay zone at 4,490ft. to the Company's successful Mitchell #4 well, which is located approximately 1,000ft. away from this new well site. The multiple confirmed pay zones will serve to extend the longevity of the well. Perforation will occur in the Gardner Limestone at 4,490ft. based on the strength of the reserve at that depth.
The Stockton #2 is expected to perform equally or slightly better than the Mitchell #4 well, which received an initial production rate of 61 barrels of oil per day (BOPD) and received a resting production rate of 45-50 BOPD during the well's first two months of production.
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Treaty Energy Corporation
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